August 18, 1998

On this day at 2:00 PM PST, my Dornier 335 finally took to the air.  It was a nice day, but a bit windy.  The wind drove off most of the guys at the field, the few that stayed to see my first flight mostly became impatient after a few false starts.  By the time of the first flight only one other club member was left.  His daughter and grandson were there as well, and it was his grandson that took the video.

I had more problems than expected getting the throttles adjusted to where both engines would come to idle together.  This took the majority of the ground time at the field.  I also had steering problems which were corrected by switching back to direct cable pull-pull linkage for the nosegear steering.  I had inserted some springs in the linkage which made it too mushy.  I also angled the main struts backward by putting spacers in the front retract mounting rail.  The combined affect of these changes was dramatic -- I now have very positive steering control even at low speed.

When I ran out of excuses, I topped off the tanks, taxied out and off she went!!!  I took the LG doors off because I had no intention of attempting gear retraction on the first flight.  I decided to follow the full scale flight test regime :-)   Take off was uneventful.  The plane was out of trim, with a little left and a lot of down required for straight and level flight.  The "down" part is probably partly because of the tail-heaviness.

Click here (or "shift-click") to download the takeoff video (1464 kb - 1.46 MB)

I made three or four circuits of the field, until the trim felt right, then one low-ish pass for the camera.

Click here to download the flyby video clip (498 kb - 0.49 MB)

After the flyby I went around to approach for landing.  It went so well, I decided to set her down.  Unfortunately I didn't realize how far "out" I was until it was almost on the ground.  I ended up a few feet off the runway.  In the video you can see the left wing rise - this was my attempt to correct :-)  The nosegear hit a bump which sheared the pivot pin!  You can see the nosegear strut and wheel flying up behind the plane in the video.  Fortunately the broken pivot pin (just a piece of 5/32 music wire) was the only damage apart from a small bend on one of the lower cowl flaps.

Click here to download the landing video clip (542 kb - 0.54 MB)

Even with the indignity of the piss-poor landing I was ecstatic that the plane finally flew and was undamaged.  I went home one very happy man!!!  I hope you've enjoyed following this project as much as I've enjoyed publishing it and getting great feedback from alot of you.  I will be posting periodic updates as the flying program continues.  As always, questions and comments welcome!

=Gary